More tales of woe debugging a KSB2

For a couple of months now, I’ve been trying to get to the bottom of the problem with my KSB2 board: the SSB adapter in my K2. Not continuously of course: I’ve had all sorts of other things to do. I’ve built the KIO2, KDSP2, and KAT2 modules as well. However, these were really just ways of resting my brain from the toil of trying to get the KSB2 working properly.

The problem manifests itself as an almost, but not quite, total absence of RF when I use SSB. The K2 works fine on CW.

Looking at the circuit, when the KSB 2 is installed, it intercepts the Rx IF path with a controlled bypass around the built in variable bandwidth IF filter. On Tx, the audio from the Mic (which is unused on CW) is processed and turned into a DSB (Double Side Band) signal at the Intermediate frequency before passing through the new filter backwards (which filters out the unwanted sideband) and then passing back into the main circuit.

The user can choose whether the received signal passes through the variable bandwidth filter on the RF board, or through the fixed filter on the KSB2 board. On transmit, only the fixed filter on the KSB2 board is used.

Thus, the fixed filter is used on Rx and Tx. I reasoned, wrongly I now suspect, that because I could choose the fixed filter on SSB receive, and hear signals, I could exclude the filter as being the source of the problem.

That left the audio processing section of the KSB2 board, and the ALC (Automatic Level Control) circuit. The latter is different from that used on CW and serves to adjust the power of the RF signal to match the level chosen by the user. Because we are talking about a single side band signal, all of the output is in the frequency-translated audio signal. The output power is directly proportional to how load you talk into the microphone. To get better “punch” to get through interference, fading and other signals, hams often raise the Mic gain to the point where they risk “over-driving” the Power Amplifier and sending out a distorted signal. This is “a bad thing” but is often by hams.

As the Mic gain is increased, the PA tries to maintain itself in a linear configuration (to minimise distortion) by “feeding back” a proportion of the output signal to an earlier stage and use that signal to lower the gain of the PA. This is the ALC signal.

Most manufacturers have a front panel meter that indicates the magnitude of the ALC signal and leave it to the user to adjust the Mic gain to a point where the ALC is at their desired level. Elecraft has chosen to adopt a smarter approach. The user uses a menu to choose a desired level of over-driving and the rig then operates automatically to maintain that level.

The K2 uses different ALC circuits on CW and SSB, so I suspected this section of the KSB2 because if it wasn’t operating properly, it could suppress the drive to the PA too much and result in insufficient RF power: exactly the symptom I was observing.

I spent ages trying to understand the ALC circuit and determining if it was working properly. To get anywhere, I had to assure myself that all the preceding circuits were working properly: Mic processing, DSB generation in the mixer and sideband removal in the filter. To do this, I needed a standard to work against.

From the elecraft list I determined that 100mV of AF at 1kHz should produce 100% of rated power at whatever level I chose. i.e. if I wanted 5W I should get 5W. I set up a signal generator to inject a 100Hz sinewave at 100mV pk to pk into the mic socket and then used my oscilloscope to trace the signal through. It soon became apparent that the problem lay after the first mixer. Although I was seeing 1V pp at the output of the first mixer, I was seeing virtually nothing in the filter.

I don’t have the test gear to debug the filter, so I have reached out to the email list for assistance.

That whole flying business

It’s easy to see why people develop such a dislike of flying.
There I was, last night, travelling down to Heathrow to stay the night at Yotel prior to departing for Detroit and Oklahoma City.
Just as I was waiting on the platform at Acton Town, because London Underground was playing silly buggers with the trains, I checked my email. Lo and behold, Delta was delaying the departure of the DL19 from 09:25 to 11:30. Just enough Delta to ensure I would miss my connection in Detroit.
Luckily I have the Delta app in my iPhone, and it’s actually pretty good. I was able to swap to another, earlier, flight, this time via Atlanta; still get an aisle seat on the first leg; and then check in.
I wasn’t so lucky with the leg from Atlanta to OKC, I’m stuck in the middle “with you?)
Yotel was an experience. Not quite the coffin experience one gets in Japan, but pretty small. That said, the bed was comfortable, it was well equipped and it was reasonably cheap. I’ll use them again.

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